SY7208互换的升压型DC-DC转换器MXT7515

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2.3V to 6V input voltage Rangel Efficiency up to 96%

26V Boost converter with 2.8A switch

current

1.2Mhz fixed Switching Frequency Integrated soft-start Thermal Shutdown Under voltage Lockout SOT23-6 Package

is a high frequency, high efficien cy DC to DC converter with an integrated 2.8A, 0.1Ω power switch capable of providing an output voltage up to 26V.The fixed 1.2MHz allows the use of small external inducti ons and capacitors and provides fast transien t response. It integrates Soft start, Comp. On ly need few components outside.

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Figure 1 Typical Application Circuit

5

1

2

3

6

IN EN

GND

SW

FB

NC

4

2.3V to 6V

Cbv 16V

1μFMXT75151.2MHZ,26V Step-up DC/DC Converter

Features

GENERAL DESCRIPTION

APPLICATIONS

MXT7515The

(Note: Do not exceed these limits to prevent damage to the device. Exposure to absolute maximum rating conditions for long periods may affect device reliability.)

6

4

1

2

5

3

(SOT23-6)

MXT7515

1 LX

Output switching node. SW is the drain of the internal N-Channel MOSFET and RDS-ON is 100m Ω. Connect the inductor to SW to

Complete the step-up converter.

2 GND Ground.

3 FB Regulation Feedback Input. Connect to an external resistive voltage divider from the output to FB to set the output voltage.Vfb=0.6V.

4 EN Regulator On/off Control Input. A logic high input(VEN>1.4V) turns on

the regulator. A logic low input(VEN<0.4V) puts the LP6218 into low current shutdown mode.

5 Vin IC Power Supply.

6 NC No Connector. MXT7515

ORDERING INFORMATION

PIN configuration Functional Pin Description

PIN PIN NameDescription

Absolute Maximum Ratings

ELECTRICAL CHARACTERISTICS

(V IN = 3.6V, T A= 25℃ C unless otherwise specified)

BLOCK DIAGRAM

Figure 3 Functional Block Diagram

The boost converter is designed for output voltage up to 26V with a switch peak current limit of 2.8

A. The device, which operates in a current mode scheme with quasi-constant frequency, is externally 1.2MHZ and the minimum input voltage is 2.3 V. To control the inrush current at start-up a soft-start pin is available.

During the on-time, the voltage across the inductor causes the current in it to rise. When the current reaches a threshold value set by the internal GM amplifier, the power transistor is turned off, the energy stored into the inductor is then released and the current flows through the Schottky diode towards the output of the boost converter. The off-time is fixed for a certain Vin and Vs, and therefore maintains the same frequency when varying these parameters.

However, for different output loads, the frequency may slightly change due to the voltage drop

across the Rdson of the power transistor which will have an effect on the voltage across the inductor and thus on on T (off T remains fixed). Some slight frequency changes might also appear with a fixed

output load due to the fact that the output voltage Vs is not sensed directly but via the SW Pin, which affects accuracy.

an internal oscillator and slope compensation, which provides better stability for the system over a wide of input and output voltages range, and more stable and accurate current limiting operation compared to boost conver has also the benefits of providing very good load and line regulations, and excellent load transient response.

To avoid mis-operation of the device at low input voltages an under voltage lockout is included that disables the device, if the input voltage falls below 2.2V

A thermal shutdown is implemented to prevent damages due to excessive heat and power

dissipation. Typically the thermal shutdown threshold is 150℃ .When the thermal shutdown is triggered the device stops switching until the temperature falls below typically 136℃.Then the device starts switching again.

FUNCTIONAL Description NORMAL Operation

Because of the quasi-constant frequency behavior of the device , the MXT7515 eliminates the need for

ters operating with a conventional PWM scheme .The MXT7515 topology

Undervoltage lockout (uvlo)

Thermal shutdown

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